Page 3 of 7 FirstFirst 12345 ... LastLast
Results 21 to 30 of 65

Thread: Trying to figure out why my reman 6-speed is failing...

  1. #21
    Forum User verified
    Join Date
    Sep 2010
    Owner Since
    August 2010

    Location
    Chicago
    Posts
    1,494
    Thanks
    46
    Thanked 57 Times in 46 Posts
    95 TD05 16G VR-4---540whp@24psi
    34XXlbs..

  2. #22
    I don't bite
    Join Date
    Sep 2010
    Owner Since
    2001

    Location
    Southern IN
    Posts
    1,996
    Thanks
    59
    Thanked 98 Times in 80 Posts
    Can't say for sure from vid, but doesn't look like the fork is seated onto the ball correctly.
    1992 Kilder Green VR4 - First 4G swap in a 3S. 2.0, auto, awd. 9.65 at 143mph. Now LS swapped. 8.52 at 162.

  3. #23
    Forum User Not Verified

    Join Date
    Sep 2010
    Owner Since
    2004

    Location
    Cape Girardeau
    Posts
    4,791
    Thanks
    365
    Thanked 296 Times in 214 Posts
    Quote Originally Posted by NOMIEZVR4 View Post
    yeah that is not on the pivot ball. Once against the pivot ball you have to smack the fork over the ball, so its retaining clip gets seated past the ball. The fork shouldn't be able to fall out of the trans once its seated on the ball.

    Parting 6 speed
    Pampena 3.5 Stroker, GTX 2867 Gen IIs, AEM Series2, oohnoo SMIC, DN Hardpipes, FIC 1650s, Walbro 525, aermotive fpr, Dejon intake pipes, Tial Q, Koyo Rad, Samco Hoses, Stoptech 332mm fronts, HKS GT4 Coilovers, Spec 4+ LW, JDM 6 Speed, Billet shift forks, Pampena brace

  4. #24
    Forum User verified
    Join Date
    Sep 2010
    Owner Since
    August 2010

    Location
    Chicago
    Posts
    1,494
    Thanks
    46
    Thanked 57 Times in 46 Posts
    I hope you guys are right...that wo be the best solution. If that ends up being it..ill be very sursurprised how the fork popped out in the first place.

  5. #25
    Forum User Not Verified

    Join Date
    Sep 2010
    Owner Since
    2004

    Location
    Cape Girardeau
    Posts
    4,791
    Thanks
    365
    Thanked 296 Times in 214 Posts
    Quote Originally Posted by NOMIEZVR4 View Post
    I hope you guys are right...that wo be the best solution. If that ends up being it..ill be very sursurprised how the fork popped out in the first place.
    I would replace the fork and ball if you bother to drop the trans.

  6. #26
    Forum User verified
    Join Date
    Sep 2010
    Owner Since
    August 2010

    Location
    Chicago
    Posts
    1,494
    Thanks
    46
    Thanked 57 Times in 46 Posts
    Both were replaced less than 10k ago...ill make the final decision after separating the trans

  7. #27
    Member Not Verified
    Join Date
    Feb 2011
    Owner Since
    2009

    Location
    Scottsbluff, NE
    Posts
    872
    Thanks
    37
    Thanked 49 Times in 36 Posts
    So would the fork not being shimmed properly potentially cause the TOB/gear rattle that annoys me so much?
    1995 Dodge Stealth R/T Turbo
    Mods: DR750s, BC Sportsman rods, Ross pistons, ACT HD 6 puck clutch, 5 speed transmission, 300M output shaft, Broomfield racing billet transfer case housings, Spectre air filter, GM 3.75" MAF w/translator, DN Pre-turbo pipes, Pampena/CX Racing dual core FMIC, M2 Performance turbo-back exhaust, Walbro 450lph E85 pump, SXPerformance fuel filter, stainless fuel feed lines, EK2 Mfg fuel rails, SXPerformance AFPR, 1000cc Bosch injectors, 99 VR4 replica ECU w/ Chrome for tuning, Kenne Bell Boost-a-Spark, Blitz SBC i-D boost controller, IPS oil cooler, Intrax springs on KYB GR2 struts, Enkei Kojin 18X9.5 +30, Nexen N3000s, 99 front end, carbon fiber steering wheel, Pioneer AVH-X2600BT, JL C2 6.5" and 6"x9" speakers, free 4 channel amp for subs (LOL), twin Alpine 10" type E subs.

    Made 608whp/631wtrq on Pampena's dyno @ 31 psi.

  8. #28
    Forum User Not Verified

    Join Date
    Sep 2010
    Owner Since
    2004

    Location
    Cape Girardeau
    Posts
    4,791
    Thanks
    365
    Thanked 296 Times in 214 Posts
    You shouldn't need to shim them unless something is worn out, but if they are not seated on the ball it would make some noise.

  9. #29
    Member Not Verified
    Join Date
    Feb 2011
    Owner Since
    2009

    Location
    Scottsbluff, NE
    Posts
    872
    Thanks
    37
    Thanked 49 Times in 36 Posts
    I'm fairly certain that it's seated on the ball properly. I'm thinking I'm probably going to order a new fork/ball for the new clutch install anyway.

  10. #30
    Forum User Not Verified

    Join Date
    Sep 2010
    Owner Since
    2004

    Location
    Cape Girardeau
    Posts
    4,791
    Thanks
    365
    Thanked 296 Times in 214 Posts
    Quote Originally Posted by DK77 View Post
    I'm fairly certain that it's seated on the ball properly. I'm thinking I'm probably going to order a new fork/ball for the new clutch install anyway.
    For as much work as it is to drop one of these trans, I would definitely do that if you suspect anything. Shimming sounds great if you like dropping the trans for fun.

Bookmarks

Posting Permissions

  • You may not post new threads
  • You may not post replies
  • You may not post attachments
  • You may not edit your posts
  •  
The 3000GT/Stealth/GTO Web History Project
3000gt.com
3000GT / Stealth International WWWboard Archive
Jim's (RED3KGT) Reststop
3000GT/Stealth/GTO Information and Resources
Team 3S
3000GT / Stealth / GTO Information
daveblack.net
3000GT/Stealth/GTO Clubs and Groups
Michigan 3S
MInnesota 3S
Wisconsin 3S
Iowa, Nebraska, Kansas 3S
North California 3000GT/Stealth
United Society of 3S Owners
3000GT/Stealth/GTO Forums
3000GT/Stealth International
3000GT/Stealth/GTO Event Pages
3S National Gathering
East Coast Gathering
Upper Mid-West Gathering
Blue Ridge Gathering