Car is finally on the dyno, but ran into issues in higher boost. Need input
After two years, I finally got my car back together and running pretty well. Took the car into FSR to have them put in the ProEFI 128 ecu and give it a tune. It sounds like the 91 octane tune went fine staying conservative and getting to 19psi where I told them to stop and switch to e85. The car put down 300whp at waste gate 7.5psi and 390whp at 12.5psi on e85 (70% ethanol content was what the sensor measured).
Mods.
-Pro EFI 128 w/ ethanol sensor and dual wideband setup
-Billet DR-650 Turbos w/Forge wastegates and green springs
-Ported heads(no idea who ported) and high rev kit
-Adjustable cam gears - Zero'd with degree wheel
-HKS DLI
- MSD Spark plug wires
-Walbro e85 pump - Hotwired
-FIC 1100CC injectors
-8AN fuel and return lines
-Fuel lab FPR
-Generic intake w/ maf deleted
-Greddy type-s bov
-RPS Max 6-puck clutch
-Bellhousing brace
-3sx downpipe
-Maximal Performance High flow cat
-Maximal Performance solid motor mounts.
Here are the issues that was emailed to me:
-The IAC motor seems very slow to respond. Maye it is just dirty or maybe it is on its way out. It has been working less and less well over the last few days.
- I suspected an issue with this after initial startup. Cleaned and it seemed to go away. Looks like it needs to be replaced now
-The rear bank is requiring about 5-7% more fuel, and the differential gets bigger as boost is going up which is why we don't want to push it more.
- Before getting on the dyno, they were trying to locate the source of an exhaust leak in the rear manifold. Could not be isolated. I gave the go ahead for tuning.
-Boost comes on nicely early but falls off drastically without tons of extra wastegate duty cycle. These cars all do that... but this one does it excessively and requires a lot of wastegate percentage as rpm gets past 4000 to keep any boost on the motor; this is indicative of a breathing issue, usually on the exhaust side.
-IAT's are getting to about 200* and the proefi is pulling timing to try to save the motor. E85 helps to cool things down a lot and IAT's will be high with small turbos but not this high. There could be a boost leak only under high boost that we are not seeing with all that stock piping in there
-The y-pipe keeps blowing off anything above 18psi
- Ebay Y-pipe :( Never had issues when running my 13g's. Will upgrade now.
-At high RPM, the dyno shows something is holding up. At low boost we can pull clean to 7k, but with boost on the motor the air fuel starts to get erratic and you can also see on the dyno graph that something isn't holing up. The most likely causes would be excessive backpressure or something in the valvetrain. Below 5krpm it does not seem to be an issue, even with lots of boost such as 25psi
Any thoughts on what could be causing these issues? Car is still on stock bottom end, intercoolers, and catback exhaust. I have not received the dyno charts yet, but will post them up when they arrive. Thinking about replacing all the rubber intercooler lines with silicone lines or moving to an FMIC. I do have a test pipe that I can throw on next time to see if it helps with the back pressure as well.
Andrew